The Foundering of the M/V MARYLAND
December 18, 1971

The Marine Weather Forecast for the Albemarle and Pamlico Sounds broadcast by the National Weather
Service, Norfolk, Virginia for 5:00 p.m., 17 December 1971 issued small craft warnings for variable winds
becoming north to northeast 15 to occasionally 25 knots later that night and continuing on 18 December
1971 clearing skies later at night, and waters becoming choppy. The 5:00 a.m., 18 December forecast
changed small craft warnings to gale warnings, for northwesterly winds increasing to 35 to 45 knots, waters
becoming choppy. At the scene of the casualty at about 9:00 a.m., 18 December 1971, the seas were 3 to 4
feet from the northwest and the wind was northwesterly, 25 to 30 knots. The water temperature was 53°F
and the computed time of sunrise was 7:00 a.m.
The Tug MARYLAND departed Charleston, South Carolina late on the afternoon of December 15, 1971
with the Barge BALTIMORE NO.2 made up ahead in the pushing mode. The BALTIMORE NO.2 was
loaded with approximately 539 short tons of paper products, which produced a draft of about 5½ feet,
freeboard of about 3 feet. The MARYLAND had refueled and filled her freshwater tanks in Charleston as
was normal practice. They carried six drums of lube oil secured on the main deck aft because the installed
lube oil storage capacity (200 gallons) was inadequate for the voyage. These drums were secured by laying
them on their sides and using wooden wedges to hold them against the bulwark under the caprail. The
drafts of the MARYLAND upon departure were approximately 7 feet forward and 9 feet aft. The voyage
up the intracoastal waterway from Charleston, S.C. to the mouth of the Alligator River was uneventful. No
problems with the machinery plant were noted and the radio was in normal operation.
At midnight on December 17, 1971, while proceeding north in the Alligator River the 6-hour watch was
changed with the second watch consisting of the Mate, Deckhand and Assistant Engineer going on duty.
At that time the Master, who had the 6:00 p.m. to 12:00 p.m. watch advised the Mate that he had received
the weather report and hat the wind was forecast to shift from the northeast to the northwest during the
night. At that time little could be sensed of the actual wind conditions because of the shielding effects of
the woods along the river. Later, as they approached the mouth of the Alligator River the Mate observed
the wind was already northwest and was getting fresh. At about 3:00 a.m. after passing through the
Lindsay Warren Memorial Bridge, near the mouth of the river, the deckhand, on the Master's orders called
the Master and first watch deckhand to assist in changing the tow from pushing to towing astern in
preparation for crossing the open waters of Albemarle Sound. The shift was made inside the bar at the
mouth of the Alligator River. During this change the Master was in control in the pilothouse and the Mate
with both deckhands worked on deck changing the rig. The Tug was then brought alongside the barge and
its 6-inch, 1200 foot, nylon towing hawser was shackled to the barge's towing bridle. With the tug going
ahead hawser was payed out until the Master indicated by means of a whistle signal to secure it. This
signal was given when about 150-200 feet of hawser has been let out upon which the Mate secured the
hawser to the towing bitt, taking enough turns on the bitt to fill it up. A hawser board was put on to
prevent the hawser chafing on the stern rail. The remaining hawser was coiled up on the hawser rack on
the stern. When the shift evolution was completed, the Mate and the second watch deckhand resumed their
normal watch. The Master and the first watch deckhand went below.
Initially, the Barge followed well and the deckhand was frequently on deck checking the adjustment of the
hawser board. He recollected that at this time all deckhouse doors were closed. At about 4:00 a.m. the Tug
with tow passed the river bar and proceeded out onto the open waters of the Albemarle Sound following the
intracoastal waterway route toward the mouth of the North River, which would call for a course of about
023°T. Upon entering the open water the tug was met by gale-force winds from the northwest and rough
seas and had to head up more toward Camden Point and the Pasquotank River, which would call for a
heading of about 340°T. The Barge began to shear from side to side and the Tug began to take water on
deck, in the well deck, faster than it could run off. Blowing spray was forming into ice and making the
decks slippery. The Mate expressed concern to the Deckhand about the towing arrangement; that he was
afraid he couldn't handle her with the barge shearing back and forth. The Deckhand offered to slack out
(lengthen) the tow line but the Mate said it was too dangerous for one man. Initially, the Deckhand felt that
conditions were not too bad and that if the Mate had stopped, he could have payed out more hawser. Later
he noted the oil drums had come lose and were rolling around in the well deck. He notified the Mate of this
condition. The Deckhand and the Mate discussed the situation for awhile. The Deckhand recalled the
Mate saying. "I don't see why in the hell he don't get up and come up here, I know he's not staying in the
bed," he said, "and I'm scared of it." In spite of his concern the Mate did not have the Deckhand call the
Master or otherwise make his concern know to the Master. The Tug continued into Albemarle Sound at
slow ahead, just holding her own.
At about 6:00 a.m. the Master and first watch Deckhand came on deck to relieve the watch. After
surveying the situation, the Master stopped the Tug to pay out more hawser. However, the loose drums
rolling around in the well deck made it impossible for the crew to safely reach the towing bitt and hawser.
Meanwhile, the wind and sea had moved the barge around and out of line with the tug. This pulled her
down aft heeling to starboard initially. The Master tried to go ahead to again bring the tug in line with the
barge. The Master tried to start the engine but it did not start. The Chief Engineer came into the pilothouse
and discussed the situation with the Master. The Chief Engineer wanted to cut the barge loose; the Master
wanted to keep the barge. Meanwhile the Tug continued to be pulled down aft, alternately heeling to
starboard then to port. The Chief Engineer went below again. Shortly thereafter the Master told the second
watch Deckhand to go to the engine room to see if he could help. He proceeded along the starboard side of
the main deck and entered engine room from the main deck. He found the Chief Engineer and the
Assistant Engineer attempting without success to start a portable gasoline bilge pump that was carried for
dewatering barges. Water appeared to be entering the engine room from the after part of the vessel, but he
could not see where it was coming from. The Deckhand did not recall the water level as being above the
deck grating. He did observe that the door to the shaft alley was open and he thought the vessel's lights
were still on; also he heard a generator still running. Shortly after the Deckhand arrived in the engine room
the Master appeared and stated that the radio would not work. No distress broadcast had been or could be
made. The Deckhand did not notice when the lights went out as it was becoming daylight.
 
The Master and the first shift Deckhand went to the boat deck to attempt to launch the lifeboat. At
this time the Tug was heeling about 45 degrees to port and the water was up to the edge of the boat deck.
When the securing gripes for the lifeboat were released, the boat rolled over and come to rest upside down
along side. The second shift Deckhand tried to assist them in righting the boat but because of the slippery
decks and the boat lunging with water washing over it they were unable to rune the lifeboat to its upright
position. By this time the entire crew was gathered on the boat deck. The Master, Cook and Assistant
Engineer has on life preservers; the Mate and second shift Deckhand had life rings; Chief Engineer and first
shift Deckhand had no lifesaving devices, the Chief Engineer commenting that he could swim better
without one. The Chief Engineer tried to open the door to the pilothouse but could not because of the
height of the water; he broke a window and went in to attempt again to use the radio. He came back and
confirmed that the radio was no longer working. The Master and Chief Engineer went aft to the area of the
towing bitt and capstan. The second shift Deckhand said they were attempting to take the hawser off the
bitt and place it to the capstan. He thought they did get a few turns on the capstan but was not sure that the
turns had been taken off the bitt. He was of the opinion that if instead they had cut the barge loose with the
fire axe, which was in a bracket on the house immediately forward of the towing bitt, the Tug may have
righted herself and survived. Shortly thereafter he say the Master in the water. He was followed by the
Chief Engineer. It is uncertain whether they fell overboard, were washed overboard, or decided to try to
swim for the barge. The first watch Deckhand was followed and was last seen swimming toward the barge
which was still attached to the Tug. During these final minutes the remaining crewmembers remained
aboard hanging onto tire fenders on the starboard side. By this time the vessel was completely over on her
port side with only the forward part of the starboard bulwark above water. As the vessel settled, the sea
action on the tires knocked or forced the remaining crewmembers into the water. After entering the water
the second watch Deckhand placed himself inside the life ring with his arms over the top. He said he felt
warmer in the water and out of the wind and that he had some ice on his clothing. He remembered being
near the barge and that the Assistant Engineer was near him. He did not attempt to go nearer because of the
heavy seas pounding against the barge. That is the last he remembered with any clarity, The next thing he
distinctly remembered was being aboard a Coast Guard helicopter. He was the only survivor.
 
The 68-foot Yacht GEORGETTA was being transported to Florida by L.R. Hastings via the intracoastal
waterway. He was accompanied by a mate and two crewmembers. At about 8:45 a.m. on December 18,
1971 the GEORGETTA reached Albemarle Sound and encountered seas of 3 to 3 feet and winds of 20 to
do knots from the northwest. Just after 9:00 a.m. as she neared the middle of the sound and sighted the
BALTIMORE NO.2. As they approached nearer the Tug MARYLAND was observed with just the
pilothouse above water. The tug rested on a southerly heading and had a list of about 10 degrees to port.
The barge was still attached to the tug and was slowly moving the tug in a southeasterly direction. The
inverted lifeboat was drifting alongside the tug and appeared attached. There was considerable debris in
the water including a life ring and two life preservers. Initially they were not sure what had happened or
when the tug had sunk as they had heard nothing about it when leaving Coinjock earlier that morning.
Then they sighted a body in a life preserver about 100 yards from the tug. It appeared obvious to them this
person was dead and knowing the short survival time under the conditions, they began looking for
survivors. As they moved closer to the barge the Deckhand was sighted in a life ring. He was thrown a
line which he held onto and was then pulled aboard the GEORGETTA. The crewmembers took him to the
cabin, removed his clothes and covered him with blankets while Hastings notified the Coast Guard by
radio. This first notification of the casualty was received by the Coast Guard Radio Station, Portsmouth,
Virginia starting at 9:08 a.m. and passed by telephone to the Rescue Coordination Center, Portsmouth,
Virginia.
The GEORGETTA returned to the body first sighted and tried to retrieve it with boat hooks but could not
due to the minimum of six foot freeboard on that yacht. Hastings secured efforts to recover the body afraid
he would rip off the life preserver and cause the body to sink.
A Coast Guard helicopter from the Elizabeth City Air Station was on scene at 9:35 a.m. and at 9:45 a.m.
lifted the survivor from the GEORGETTA and transported him to Albemarle Hospital in Elizabeth City.
During the time the helicopter was gone the GEORGETTA continued to search concentrating downwind of
the tug and barge, At about 10"30 a.m. the barge broke free of the tug and began drifting to the southeast.
At about 12:50 p.m. the Coast Guard Patrol Boat CG-30475 from Light Attendant Station, Coinjock, NC
arrived and joined the search. It was directed toward the know body by the GEORGETTA and recovered
it. The body was identified as that of the Master.
The Coast Guard air and sea search for the missing men was continued through 21 December 1971 without
success. At that time active search was suspended. Periodic searches, searches during other activities, and
searches by local law enforcement agencies along the surrounding beaches continued until all bodies were
recovered on 11 January 1972. Six souls were lost.
CONCLUSIONS
A United States Coast Guard Marine Board of Investigation Report was released on 11 July 1974. The
major conclusions were as follows:
- The casualty was caused by the failure of the Master to cut the barge adrift. Had the towline
been cut at any time during the significant time period which elapsed between the
unsuccessful efforts to restart the tug's engine and the point where progressive flooding would
have resulted in capsizing even without the tripping force of the tow, the tug could have
remained afloat. Relieved of the tripping and stern pull-down forces of the wind-driven tow,
the initial flooding could have been controlled. The reluctance of the Master to cut free the
barge must e attributed to psychological factors related to the traditional blemish on the record
of a master who abandons his tow.
- The failure of the engine to restart after initial efforts to pay out the towing hawser were
abandoned was caused by fouling of the propeller by the towing hawser. A bight of the end
of the hawser, initially stowed on the well deck hawser grating was washed overboard through
the aftermost starboard freeing port at some time after leaving the mouth of the Alligator
River and encountering heavy weather but prior to stopping the vessel to lengthen the hawser.
When stopped, the drift of the tug caused the bight of trailing towline to tend under the tug in
way of the propeller where it became fouled in the propeller when the direct driven diesel
engine was cranked over for starting. Succeeding turns collected around th propeller shaft,
between the propeller and stern frame until sufficient restraining force developed to prevent
further cranking of the engine. Without propulsion the tug was towed stern first, heeling
alternately to one side or the other, by the still attached wind-driven barge. This towing
action typically pulled the stern down and under. Flooding initially occurred through the
loose or open scuttle to the lazarette space thus further submerging the stern. Simultaneously,
or shortly thereafter, water began to enter the machinery space through loosely closed
portholes and weather deck doors opened during the aborted towline lengthening operation.
Although initial flooding of the engine room was slow, electrical power was lost almost
immediately. The initial entry of water must therefore have grounded out the switchboard
rendering the electric bilge pump, radio and other essential electrical equipment inoperative.
Without propulsion or electrical power and with the tripping of the stern pull-down forces of
the towline still in effect, flooding of the machinery space progressed at an increasing rate
until insufficient stability remained to resist capsizing forces of the wind and tow. The tug
finally laid on her side but still afloat. In this position she experienced rapid flooding of other
spaces, finally setting to the bottom in a more or less upright position with the barge still
attached by the towline slowly dragging her over the bottom until chafing action parted the
towline.
FACTS, CREDITS & VESSEL DATA
- The sole survivor was John S. Williams, Deckhand, holder of a Merchant Mariner's
Document endorsed for Ordinary Seaman, Food Handler. As a result of the casualty, he was
hospitalized for four days for treatment of exposure.
- Name of Vessel MARYLAND
Official Number 279563
Service Towing
Gross Tons 166
Net Tons 89
Length 96.2 feet
Breadth 22.0 feet
Depth 8.8 feet
Propulsion Diesel/Single Screw
Horsepower 690
Home Port Norfolk, Virginia
- Document Source for this article:
Marine Casualty Report:
FOUNDERING OF THE M/V MARYLAND
IN ALBEMARLE SOUND, NORTH CAROLINA
ON 18 DECEMBER 1971 WITH LOSS OF LIFE
U.S. COAST GUARD
MARINE BOARD OF INVESTIGATION REPORT
RELEASED 11 JULY 1974
- Images Provided Courtesy of:
WAFF CONTRACTING, INC.
PO Box 237
Edenton, NC 27932
(252) 482-7071
info@waffcontracting.com
http://www.waffcontracting.com
RAI / 02 June 2010
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